Troubleshooting: Difference between revisions

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== AFRC 20230 20235 20360 ==
=== Input Issues ===
==== Narrowband O2 reading is 0 or otherwise incorrect ====
*Note that the O2 reading will not show up until the run signal is met, under AFRC “Setup” -> “Run Signal Trigger”
*If the AFRC is displaying the O2 reading in units of lambda (λ), the sensor type setting is incorrect. Go to the AFRC setup and change the O2 type to Narrowband.
*With the AFRC plug disconnected, the AFRC screen should show an O2 reading of around 450-550 Mv. If not (assuming the run signal is met), the board may be damaged.
*If above passes but goes to zero when the sensor is plugged back in, unplug the harness at the sensor end. Once again the reading should go to 450-550 Mv.
**If not, the harness is grounded out, or the DPV and O2 harnesses are swapped.
*If above passes, check with a multimeter on the loose harness going back to the panel that V DC from pin “B” to any ground is around 0.45-0.55 volts. If it is not, the harness itself is miswired or not landed correctly.
*If above passes but the reading is still zero when plugged in, then the O2 sensor itself is damaged, or the O2 reading is truly very lean
*If the sensor is consistently low (lean), the sensor may be at its lifetime
==== Wideband sensor incorrect or erratic====
*Note that the O2 reading will not show up until the run signal is met, under AFRC “Setup” -> “Run Signal Trigger”
*If the AFRC is displaying the O2 reading in units of mV, the sensor type setting is incorrect. Go to the AFRC setup and change the O2 type to wideband.
*Verify all three shield wires are connected to the ‘drain’ terminal
*If possible, a continuity check can be done from the plug end to the board. The wiring should be:
**Pin 1: White
**Pin 2: Orange or Blue
**Pin 3: Red
**Pin 4: Black
**Pin 5: Green
**Pin 6: Yellow
====Thermocouple Reading Incorrect====
*If the TC reading is consistently low only with the engine running, the thermocouple may be picking up noise. If available, a .01uF capacitor in the terminal block may fix the reading. If an annunciator is present, the TC can be connected to the annunciator instead and it will be shared with the AFRC if named properly.
*Verify the polarity of the TC wires are correct
====Analog input incorrect====
*(If the sensor has a plug) Disconnect the plug and check the two pins on the harness going back to the panel with a voltmeter. One of the two should have +12V to a chassis ground. If not, the harness or panel wiring has a break.
*With the sensor re-connected, check the signal pin to ground (e.g. pin 9 to ground). It should read around 0.5 V – 3.3 V.
*If above does NOT pass, try connecting the signal wire to another analog input (e.g. move pin 9 to 12 on AFRCA). If it starts working, there is a problem on the AFRCA board with the original input pin.
*If the other pin does not work either, the cause is likely one of the following:
**There is a break in connection between the module and the end of the harness
**The wires are misconnected or backwards
**The sensor is bad
===Output Issues===
====DPV does not move or may not be moving====
*Unplug the DPV at the module and on the unplugged phoenix connector check the resistance from A to D, and the resistance should be roughly 50 ohms. Similarly, the resistance from B to C should be 50 ohms. If not, there is a break in the connection in the harness or at the valve itself. The O2 and DPV harnesses could also be swapped.
*Run the DPV in manual on the EIM open and closed, and see if the O2 reading shifts. If so, the DPV is operating. If closing the valve causes the engine to go rich, then some of the wiring is swapped and the valve is operating backwards.
*If the first step above passes but the DPV is definitely not moving, the board itself may be bad
===Control Issues===
====DPV limit stays at/near maximum, or AFRC throws “loss of control” alarm====
*Adjust the fuel pressure to get the valve more in the center of the range
*Verify in manual mode that the DPV is moving in the correct direction
====In ‘Autocontrol’ mode, the AFRC tends to rest very rich====
*Lower the ‘postcat lean threshold’ 50-100 points
*Adjust rich/lean setting up
== Ignition 20270 ==
== Ignition 20270 ==



Revision as of 20:48, 21 July 2023

AFRC 20230 20235 20360

Input Issues

Narrowband O2 reading is 0 or otherwise incorrect

  • Note that the O2 reading will not show up until the run signal is met, under AFRC “Setup” -> “Run Signal Trigger”
  • If the AFRC is displaying the O2 reading in units of lambda (λ), the sensor type setting is incorrect. Go to the AFRC setup and change the O2 type to Narrowband.
  • With the AFRC plug disconnected, the AFRC screen should show an O2 reading of around 450-550 Mv. If not (assuming the run signal is met), the board may be damaged.
  • If above passes but goes to zero when the sensor is plugged back in, unplug the harness at the sensor end. Once again the reading should go to 450-550 Mv.
    • If not, the harness is grounded out, or the DPV and O2 harnesses are swapped.
  • If above passes, check with a multimeter on the loose harness going back to the panel that V DC from pin “B” to any ground is around 0.45-0.55 volts. If it is not, the harness itself is miswired or not landed correctly.
  • If above passes but the reading is still zero when plugged in, then the O2 sensor itself is damaged, or the O2 reading is truly very lean
  • If the sensor is consistently low (lean), the sensor may be at its lifetime

Wideband sensor incorrect or erratic

  • Note that the O2 reading will not show up until the run signal is met, under AFRC “Setup” -> “Run Signal Trigger”
  • If the AFRC is displaying the O2 reading in units of mV, the sensor type setting is incorrect. Go to the AFRC setup and change the O2 type to wideband.
  • Verify all three shield wires are connected to the ‘drain’ terminal
  • If possible, a continuity check can be done from the plug end to the board. The wiring should be:
    • Pin 1: White
    • Pin 2: Orange or Blue
    • Pin 3: Red
    • Pin 4: Black
    • Pin 5: Green
    • Pin 6: Yellow

Thermocouple Reading Incorrect

  • If the TC reading is consistently low only with the engine running, the thermocouple may be picking up noise. If available, a .01uF capacitor in the terminal block may fix the reading. If an annunciator is present, the TC can be connected to the annunciator instead and it will be shared with the AFRC if named properly.
  • Verify the polarity of the TC wires are correct

Analog input incorrect

  • (If the sensor has a plug) Disconnect the plug and check the two pins on the harness going back to the panel with a voltmeter. One of the two should have +12V to a chassis ground. If not, the harness or panel wiring has a break.
  • With the sensor re-connected, check the signal pin to ground (e.g. pin 9 to ground). It should read around 0.5 V – 3.3 V.
  • If above does NOT pass, try connecting the signal wire to another analog input (e.g. move pin 9 to 12 on AFRCA). If it starts working, there is a problem on the AFRCA board with the original input pin.
  • If the other pin does not work either, the cause is likely one of the following:
    • There is a break in connection between the module and the end of the harness
    • The wires are misconnected or backwards
    • The sensor is bad

Output Issues

DPV does not move or may not be moving

  • Unplug the DPV at the module and on the unplugged phoenix connector check the resistance from A to D, and the resistance should be roughly 50 ohms. Similarly, the resistance from B to C should be 50 ohms. If not, there is a break in the connection in the harness or at the valve itself. The O2 and DPV harnesses could also be swapped.
  • Run the DPV in manual on the EIM open and closed, and see if the O2 reading shifts. If so, the DPV is operating. If closing the valve causes the engine to go rich, then some of the wiring is swapped and the valve is operating backwards.
  • If the first step above passes but the DPV is definitely not moving, the board itself may be bad

Control Issues

DPV limit stays at/near maximum, or AFRC throws “loss of control” alarm

  • Adjust the fuel pressure to get the valve more in the center of the range
  • Verify in manual mode that the DPV is moving in the correct direction

In ‘Autocontrol’ mode, the AFRC tends to rest very rich

  • Lower the ‘postcat lean threshold’ 50-100 points
  • Adjust rich/lean setting up


Ignition 20270

Input Issues

General Input Checking

On the ICM home page, the ‘Input Information’ box can be selected to view the position input information. While cranking, both the flywheel teeth input and the index input (either another MPU or the hall sensor) should be shown as moving. Also, the “Additional Debug” button can be checked on this page both before and after cranking to see if the “Input Counts” have increased.

RPM Reads "0" when cranking

A general diagram of the MPU circuit is shown below

Icm mpu.png

While the flywheel turns, the MPU generates an AC voltage wave where the frequency is equal to the speed of the flywheel movement.

  • Verify that the flywheel teeth MPU is plugged into the correct circular connector. The ICM box has two circular connectors for MPU- one for flywheel teeth and one for the index.
  • If above is verified correct, unplug the MPU and use a multimeter to measure AC Volts across the two MPU wires while cranking. It should show around 2-10V AC. If less is shown, then one of the following may be the cause:
    • The MPU is bad
    • The connection to the plug is bad
    • The engine is cranking too slowly to generate proper voltage
    • A stronger MPU is needed
    • The MPU is not close enough to the flywheel (typically should be ¼ to ½ turn out)
  • If test above passes, plug the MPU back in and check the AC voltage at the ICM phoenix plug (pins 22/23) with the phoenix plug removed. Again it should be roughly 2-10V AC during cranking. If less is shown, there is a wiring problem in the harness or box preventing the signal from reaching the ICM.
  • If test above passes, plug the phoenix plug back into the ICM and measure the AC voltage again while cranking. If it is low in this case, the ICM MPU input may be damaged
  • Verify that the flywheel teeth setting is correct

Hall sensor not moving

If the input information screen shows the hall sensor not moving, or the alarm “Hall Disconnect” is thrown when using a hall sensor, then the board is not seeing the hall sensor at all. Typical system wiring diagrams are shown below. Verify that pin 14 is used for hall sensor power, and not pin 25.

330x Hall sensor Wiring:

Icm hall 330x.png

Threaded hall sensor wiring:

Icm hall threaded.png

  • With ICM powered, unplug the hall sensor at the engine (or aux pickup) and verify the following on the harness end:
    • 330xB hall sensor:
      • Pin A- DC V to ground should be 12 V
      • Pin B- Resistance to ground should be < 1 ohm
      • Pin C- DC V to ground should be 5 V
    • Aux pickup connector
      • Pin A- Resistance to ground should be < 1 ohm
      • Pin B- DC V to ground should be 5 V
      • Pin D- DC V to ground should be 12 V
    • Threaded hall sensor with 4-pin weatherpak (checking on weatherpak):
      • Pin B- DC V to ground should be 5 V
      • Pin C- Resistance to ground should be < 1 ohm
      • Pin D- DC V to ground should be 12 V
  • If any of the tests in above fail, there is wiring or connection issues in the harness or box.
  • If above passes, jump a wire from ground to the pin on the connector that is listed as “DC V to ground should be 5 V” above. For each time grounding that pin, the hall sensor input counts on the input status screen should increase. (Note: The input count dialog aka ‘Additional Debug’ has to be closed and re-opened to update the input counts).
    • If this does not work, there is a connection problem between the end of the harness and the ignition board, or a problem with the ICM board itself.
  • If above passes, remove the hall sensor and move a magnet to see if the input counts increase. For the aux pickup, plug back in and spin the engine or remove and spin the input shaft manually.
    • If this fails, the hall sensor itself may be bad

TDC MPU Index not moving

If using a mag pickup for the TDC index, follow similar troubleshooting steps as Flywheel teeth mpu above, except at the board the wires run into pins 20/21.

Shutdown pin input not working / Ignition is not in "External shutdown" when engine is off

The general wiring of the shutdown circuit is shown below.

ICM sd wiring.png

  • Disconnect the annunciator plug (or disconnect the shutdown wire at the annunciator). Jump the disconnected wire (or Pin 9 on the disconnected phoenix block) to ground. Within a few seconds the ICM status should change to “Externally disabled”.
    • If above passes, then the problem is with the annunciator or the wrong annunciator pin is used
  • If above fails, unplug the phoenix connector on the ICM board (13-18). Jump pin 17 on the board itself to ground, and see if the status changes to “Externally disabled”.
    • If above passes, the problem is with a wiring connection between the ICM board and the annunciator pin. Check each of the connection points in the drawing above.
    • If above fails, the problem is in the ICM board itself.

Hall sensor or TDC index moving, but erratic or not resolving correctly

  • Verify that the ignition setup is correct. The inputs shown as active in step 1 of ignition setup should be the same as the sensors on the engine.
  • Verify that all the connections are well established (see wiring info in “Hall sensor not moving” above)
  • Route the hall harness as far away from the coil harness and other noise sources as possible
  • If using the flange mounted hall sensor, make sure that the sensor is well seated against the engine.

Output Issues

One or more coils do not fire

  • If no coils fire, first verify on the input status screen that the ignition is even trying to fire. If not, troubleshoot the inputs using the above sections
  • Make sure the ICM status shows ‘Ready to Start’ before starting the crank
  • Using the Ignition “Setup and Testing” -> “Engine Off Diagnostics and Testing” each cylinder can be tested with the engine off. During each test, every coil positive pin should be energized with battery voltage, but only the coil under test will have its negative pin grounded out during fire.
    • If the ICM shows the test in progress but there is no voltage at the positive pins, there is a connection issue in the harness or ICM Box
    • If the ICM shows the test in progress but the pin is not firing, try a few other coils. The negative wire may be mixed up with another coil.
    • Swapping a coil/secondary/plug with a neighboring cylinder may reveal a bad part

Coils fire in test, but when cranking engine one or more do not fire

  • Make sure the input status shows that the tooth count is good. If the index input is incorrect some coils may be prevented from firing
  • Make sure the dwell time is set long enough to fire the plugs while the cylinders are compressed
  • Check to see if any secondary leads appear to be arcing out. The voltage demand in compression will be higher than during engine off testing, and misfires will be more likely.

ICM Module does not appear on EIM/DCT screen

  • Verify that the module power light is on, if not check power wiring and fuses
  • Check that the CAN termination switches are in the correct direction. Any module with only one can connection (at the end of a chain) should have the switch terminated. Any module in the middle with two connections in the can pins should have the switch unterminated. The ICM will always be at the end of the chain since it is on the skid. The CAN connection is in the power/comm harness (blue/green/yellow wires), and typically runs to terminal blocks that jump to the next module.
  • With all modules plugged in and everything powered off, checking the resistance between CANH and CANL of any module should read about 60 ohms. If the ICM is at the end of a chain and it is unplugged, the resistance between the two pins should go to 120 ohms.
  • If the above is not true, there is likely a problem with the termination switch positions, or one of the two can wires has a disconnect somewhere

ICM module resets during operation or throws reset code

  • Verify that there are good ground connections directly to the skid. If needed, run a chassis wire from the ICM board to the engine block.
  • Occasionally the ICM will reset on shutdown when all the coils are shut off, after the engine shuts down for another reason.
  • Verify that nothing is loose in the power wiring / fusing
  • The board may have a hardware issue that causes resets (contact EMIT)

Control Issues

Spark durations are abnormally low on one or more cylinders

  • Spark plug could be fouled or the gap too wide
  • The dwell time may not be set high enough for the compression of the engine
  • The fuel mixture may be overly lean

Spark durations are abnormally high on one or more cylinders

  • The spark plug gap could be too narrow
  • The secondary circuit could be grounded out or misfiring. Replace the secondary lead if needed.
  • The compression on the cylinder may be low
  • The dwell time may be set too high

Ignition displays “Bad Configuration”

  • Update to the latest ICM version to make sure any bad config values are cleared out
  • Make sure there aren’t two cylinders firing the same pin

Timing light shows a timing that does not match what is displayed on the screen

  • Use the Ignition “setup” -> “Timing Calibration” screen to calibrate the timing.

Ignition displays “Bad peak count” fault and/or has erratic timing

  • See the debug steps above under “Hall sensor or TDC index moving, but erratic or not resolving correctly”
  • If the flywheel has any broken teeth, make sure that the configuration is set to the original number of flywheel teeth
  • Make sure the flywheel is relatively clean of debris

Governor / Speed Controller 20310

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GOV Input Issues

RPM Reads “0” when cranking

General input wiring is shown below.

GovmpuBasic.png Wiring to module

GovMpuPanel.png Wiring through panel terminal block

While the flywheel turns, the MPU generates an AC voltage wave where the frequency is equal to the speed of the flywheel movement.

If no ICM is present on the system, OR if an ICM is present but two flywheel teeth MPUs are used:

  • Unplug the MPU and use a multimeter to measure AC Volts across the two MPU wires while cranking. It should show around 2-10V AC. If less is shown, then one of the following may be the cause:
    • The MPU is bad
    • The connection to the plug is bad
    • The engine is cranking too slowly to generate proper voltage
    • A stronger MPU is needed
    • The MPU is not close enough to the flywheel (typically should be ¼ to ½ turn out)
  • If test above passes, plug the MPU back in and check the AC voltage at the governor phoenix plug (pins 16/17) with the phoenix plug removed. Again it should be roughly 2-10V AC during cranking. If less is shown, there is a wiring problem in the harness or panel preventing the signal from reaching the governor.
  • If test above passes, plug the phoenix plug back into the governor and measure the AC voltage again while cranking. If it is low in this case, the governor MPU input may be damaged.
  • If above passes, check these final items:
    • Verify the flywheel teeth setting is correct
    • Verify there is no alarm for ‘governor sw error’ indicating the test version is installed
    • The governor board may be bad

If an ICM is present on the system

Often, the ICM Tachometer output is wired into the governor MPU input as shown. Note that the Tach goes to one of the governor MPU inputs, and the other is not connected (floating).

GovMpuICM.png

  • Navigate to Ignition ‘Setup and Testing’->’Timing Calibration / Tachometer Output’, and verify that the tachometer pulses per revolution is set to the number of flywheel teeth. Verify also that both the ICM and governor main setups have the flywheel teeth setting correct.
  • If above is correct, check where the tach wire lands in the panel (which is the black wire on the ICM comm harness), and check the DC Hz on the tach wire (removed from terminal block) to ground. During crank, it should go from 0Hz to around 500Hz – 2KHz. If it does not:
    • Verify that the tach connection in the ICM box is secure
    • The ICM box may have a damaged tach circuit
  • If above passes, re-connect the tach wire and check the same DC Hz on the MPU+ pin on the governor (16) during crank then the MPU- pin (17) during crank. One of the two should have the 500Hz – 2KHz during crank. If not:
    • A connection may be miswired or missing from where the tach lands back to the governor module. A continuity check from the tach terminal block back to pins 16/17 of the governor can help track down a missing connection.
    • The governor board MPU input may be damaged

MPU reads more than 0, but is not correct

If the MPU is reading a faulty RPM, verify the following

  • Make sure the flywheel teeth setting is correct
  • If an ICM is present on the system, verify that at the page Ignition ‘Setup and Testing’->’Timing Calibration / Tachometer Output’, the tachometer output pulses per revolution is set to the number of flywheel teeth
  • Verify that all connections are secure at the MPU plug and where wires land in the panel and governor module
  • The MPU may not be screwed in far enough. Verify it is within ½ to ¼ turn of the flywheel.
  • The MPU harness may be picking up noise. Make sure it is routed away from noise sources, and the drain wire is connected to ground.

The throttle position does not show around 0% position when the engine is off

  • The throttle may need to be re-calibrated. Navigate to Governor ‘Setup’ -> ‘Throttle Calibration’ and hit ‘calibrate now’.
  • If above does not fix the issue, see if the position appears to change at all while the calibration is taking place, if not, go to ‘Throttle not moving’ below
    • If the position is moving but the calibration still does not complete successfully, go to ‘throttle feedback problems’ below

Throttle Feedback Problems

The Bosch throttle bodies use four feedback lines (terminals 20-23 on the governor module). Typical voltages are shown below. The actual feedback voltages (20/21) will vary ~0.3V between motors. The motor can be moved through calibration or manually.

GovV.png

  • If voltage does not appear on 22 (5V) but the governor module is powered up, there is likely a problem with the governor board
  • If voltage does appear on 22, but does not appear on 21/20, check for a bad connection somewhere between the module and the throttle body
  • If voltage appears on only one of 21/20, the other connection has a break between the module and the throttle body
  • If the voltages are roughly correct and the motor can move, but the calibration is still failing, it could be because of a problem with the pcb (preventing the reading of the voltage) or a bad throttle body (where the feedback potentiometer is not functioning correctly).

Panel switches reading incorrectly

If the EMIT Brain is not Used

Each of the panel switch inputs (pins 8-14 on the governor module) operate by closing to ground. At any given time one of the inputs Idle/Auto/Manual should be closed to ground, and sometimes one of the Speed+/- may be as well.

If no mode is closed to ground, the governor defaults to ‘idle’, so the idle pin (8) is not connected in panel applications.

  • If the module is not reacting properly to the switches, check continuity to ground on each of the input pins as the switch is moved in/out of the position related to that pin label. The pin should be connected to ground (showing <2 ohm) when the switch for that pin is selected
    • If this test fails, look for wiring errors or breaks in the switch blocks. Green blocks are normally open and red blocks are normally closed.
    • If this test seems to pass but the governor still shows the wrong switch position, the module may be bad. Try unplugging the two phoenix blocks for the switches and jumping pin 11 (ground) to one of the mode selects to see if they change the mode.

If the EMIT Brain is Used

The panel switches will wire to the brain and it will send the positions to the speed module. See the troubleshooting section for Brain - Switch issues.

GOV Pressure Sensor(s) not reading any value

Typical sensor wiring is shown below for one sensor. If an annunciator/Brain is present, the sensor will likely not be wired to the governor and this section can be skipped.

Ts 1 1 6.png

For an EMIT harness, the colors will be as shown above with red on a PWR OUT and the white wire into the required input. If a bare sensor without a plug is wired in, a black wire will be used for the signal wire instead of white. From the governor home page, the ‘Sensors’ button will show the raw and scaled value for each analog input.

  • (If the sensor has a plug) Disconnect the plug and check the two pins on the harness going back to the panel with a voltmeter. One of the two should have +12V to a chassis ground. If not, the harness or panel wiring has a break.
  • With the sensor re-connected, check the signal pin to ground (e.g. pin 31 to ground). It should read around 0.5 V – 3.3 V.
  • If above does NOT pass, try connecting the signal wire to another analog input (e.g. move pin31 to 32). If it starts working, there is a problem on the governor board with the original input pin.
  • If the other pin does not work either, the cause is likely one of the following:
    • There is a break in connection between the module and the end of the harness
    • The wires are misconnected or backwards
    • The sensor is bad

Pressure sensor reads a value, but it is not correct

If the pressure sensor is reading an incorrect value, it is most likely caused by the scaling not being set correctly. This can be adjusted in Governor “Setup” -> “Sensor Setup”.

Pressure sensor is connected to the Brain / Annunciator but does not share to the governor

If the annunciator is connected to the normal pressure sensors, it should be sharing the suction and final discharge stage values to the governor. If it does not:

  • Make sure the built-in names for the stages are used on the annunciator so that the system knows how to sort out the input. E.g. choose ‘Suction’ for first stage suction instead of using a custom name like ‘First stage suction’.
  • Make sure the module firmwares are relatively up to date.

Output Issues

Governor does not show up on EIM or DCT

  • Verify that the governor is powered up and running. The Power status LED should be green, and the STATUS led should be pulsing green every second or so.
    • If not, check power wiring. If the STATUS led is not pulsing and the module is not showing up on the EIM/DCT, the board could be non-functional because of electrical damage.
  • Check that the CAN termination switches are in the correct direction. Any module with only one can connection (at the end of a chain) should have the switch terminated. Any module in the middle with two connections in the can pins should have the switch unterminated.
  • With all modules plugged in and everything powered off, checking the resistance between CANH and CANL of any module should read about 60 ohms. If the governor is at the end of a chain and it is unplugged, the resistance between the two pins should go to 120 ohms.
    • If the above is not true, there is likely a problem with the termination switch positions, or one of the two can wires has a disconnect somewhere

Throttle not Moving

  • Unplug the throttle body connector at the governor module (phoenix block with numbers 20-25). Check the voltage between pins 24 and 25 (MOTOR-, MOTOR+) on the module. When someone hits ‘Calibrate Now’ on the governor calibration screen, for a couple seconds there should be around 12V between the two pins. If not, the board likely has an issue.
  • If above passes, check the resistance between on the unplugged phoenix connector between pins 24 and 25. The resistance should show around 1-5 ohms.
    • If it does not, there is a connection issue between the throttle body and the module. Verify wiring from the phoenix connector to any terminal blocks, and from there to the end of the harness. Verify that the harness is plugged in.
    • If showing around 1-3 kohms, it is possible that some of the wires are swapped or harness mixed up.

Control Issues

RPM is erratic

  • Navigate to governor “Setup” -> “Engineering Setup”. Try adjusting the “Throttle gain setting” up and down (especially up). If this does not have an effect, return to “50”. Similarly try increasing or decreasing the “RPM gain adjustment”. In general, increasing the RPM gains will cause faster response but potentially lower overshoot. Lowering the RPM gains leads to slower response but less overshoot.
  • Verify that fuel pressure and AFR are relatively steady
  • Make sure there is not an active alarm for throttle feedback error. If there is, recalibrate the throttle with the engine off.
  • If the throttle body has been in use for a long time, the gear may have enough wear in it that the throttle plate has too much slack

Engine will not start

  • While cranking, verify that RPM is showing up. If it is not, go to section above “RPM Reads ‘0’ when cranking”
  • If above is ok, verify that the throttle goes to an open position during cranking. If not, go to “Throttle not moving” above.
  • If above is ok, the starting throttle may need to be adjusted. This is under governor “Setup” -> “Engineering Setup”.

EIM 20200

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Screen boots to the EMIT logo, but is stuck there

  • Usually this is an issue with the internal memory and must be repaired by EMIT
  • The SLC-SD card lock may be grounded against the case
  • The SLC-SD card itself may have an issue

Screen boots past the EMIT logo, but the application does not start

  • Usually this will require repair
  • An SLC-SD card from a different EIM was used and the encryption does not match (Cards cannot be swapped between EIMS)
  • The SLC-SD card may be bad

Screen is always black

  • Try cycling power on the screen
  • Verify that the input voltage is between 12 and 30 VDC
    • If input power is good but the green power LED does not come on, the EIM needs repair
  • Behind back cover, verify that the backlight connection is in all the way

Eim bl.jpg

  • If all of the above is ok and there is still no boot, the EIM needs repair. It is most likely an issue with the SLC-SD card.

Touch screen input does not detect press in correct location

  • The touchscreen may need to be re-calibrated under “System Settings” -> “About” -> “Calibrate Touch Screen”
  • If debris accumulates under the bezel it can screw up touch detection. Cleaning around the bezel can fix this issue.
  • Sometimes the screen bracket is too tight causing this issue. Remove the back cover and loosen the left and right screen screws slightly (3 per side that go into bezel)